Shopvac bearing oiling / disassembly
The bearings on this one have started making a squealing whining type noise for the first second or so after it's turned on and sometimes when it's turned off. Unless the bearings get oiled, they will soon squeal more and destroy themselves. So it's time to open this one up and oil it.
Chances are, the problematic bearing is the top bearing, and just applying some oil to it will fix the problem. The bronze sleeve bearing is surrounded by some felt soaked with oil, which would ideally also get re-soaked with oil. I suppose if I put the unit upside-down and squirted some oil onto the other side of the bearing mount, that could do it.
But this time, I proceeded to take the whole motor unit apart. Not really necessary, but I wanted to show how these go together.
With the screws that I removed already, the whole blower unit pops out of the red top cover part. The parts that are red on this ShopVac are different between different models, but the internal blower units tend to be nearly identical.
Here removing three more screws to pop off the cover over the blower.
This is the blower after removing the cover. The blower impeller is held on either by a nut (which is best removed with a nut driver in an impact diver) or by a little spring clip, which is best pried off by lifting it with a flat screwdriver near the center.
After the clip or nut is removed, the rotors may require a bit of prying too.
Take note of how the rotor fits into the flanges on it and be sure to put it back together the same way.
Here I took two screws out of the motor to take the back bearing off.
Whatever you do, don't get any oil on the commutator (the part made out of copper segments, right next to the bearings in this photo). If you get oil on the commutator, it starts to burn from the sparks and ruins the commutator.
The trickiest part was getting the rotor back into the motor. I used a small screwdriver to jam one of the spring loaded brushes back and used another screwdriver to hold the other brush back while inserting the rotor. Then inserting the rotor again. The brushes, if pulled fully back, can jam, so I had to wiggle one of them to get it to come forward again. Getting the rotor back in is tricky. I don't recommend removingthe rotor from the motor!
After that, the rest of the assembly was just the disassembly in reverse. One thing to watch for - where will the cord come out? There are two orientations for how some of the parts go together, but only one has the power cord lining up with where it should come out.
I have five ShopVacs, none of which I bought new. Most were picked up from the curb on garbage day. Usually, there isn't much wrong with them. Often, they are plugged up with dust, sometimes the internal thermal fuse is blown, and more often than not, they require oiling. So if you have a ShopVac that makes a funny noise, or come across a thrown out one, chances are, it only needs a little bit of work to make it usable again.
A question I'm often asked is how to make use for a ShopVac motor for a homemade machine. The answer is - you can't. ShopVac motors aren't usable for anything else. They run far too fast to be usable for a homemade machine. They are also much too loud and don't last very long.
I had that shopvac apart for oiling in 2016. 3 1/2 years later, the bearing chatter got to a point again where I could not ignore it, so time to re-oil.
But in the mean time, I got one of those rare useful YouTube comments. A viewer pointed out that he just drills a hole above the bearing, so he can re-add oil to the top bearing. The bottom bearing is a ball bearing and doesn't run out of oil like the top bearing does.
So that's what I did this time. There is no need to re-seal the hole on this one because that cover is open on the sides anyway, and lots of air blows through, so it's not like I have to worry about air flowing or debris - there's lots of air flowing through there regardless.
This was going to be just an aside of another video, but that video was already getting too long, so I edited that bit into its own very short video.
Another similar shopvac repair by Art Mulder